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Old 10-28-2019, 08:42 AM   #1
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The 2019 $2000 Challenge is complete. I placed 18th out of 57 cars that made it through scoring. I had a great time and learned a lot. With the V8 installed next year I think this car can truly be competitive.

I didn't push the 2.5L engine to the breaking point, but I could tell it was weakening. After every run, it needed to cool down for 20-30 minutes to de-pressurize and refill the coolant tank. On my first drag run with the car floored the whole way, running to a 7k redline, it only got a 16.1 1/4 mile. With a 50 shot of nitrous it did 14.6 with the Tiptronic shifting at 8k rpm. The 150 shot would have been glorious, but I was worn out from a long day. My wife convinced me to let the engine live and we called it a night.

Later this week I'll detail the modifications to the car, to wrap this up as a 'build thread'. I'll post the build for next year under a new title. Here's a few pics from the Challenge.

Prep in the paddock:


Topping coolant. Extra plastic tank (Audi) catches the drainage.


Tight corner in the autocross.


Danny Shields completing a run in my car. Great to get feedback from a pro driver.
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Old 10-30-2019, 08:03 AM   #2
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A few mod details.
I got rid of the heavy stock muffler and welded some pieces cut from a scrapped exhaust onto the 'C' pipes. I would have deleted the cats too, but considering the value vs the time available, I left them. It sounds great at high revs, but not too loud at idle.


For the single radiator, I cut the fork out of the long tubes and used hose to join the elbow on.


I had a problem with the Toyota radiator. The engine I have over-pressurizes the cooling system and the radiator cap was a weak point that leaked. I went to a single stock radiator. The way I have the radiator positioned it has good, direct airflow without bends and restrictions. The temp stayed on the '8' in 180, but I still lost coolant from the pressure relief valve in the tank.


I installed a lawnmower battery in the stock position with 3/8 rod to tie it down. It worked great, was light weight, and cost about $25.


The nitrous oxide system from Nitrous Express, was easy to install and worked great. Nitrous tank in the trunk and fuel from the fitting on the fuel rail. I had ordered a system with a mechanical wide-open-throttle switch, but they sent one that works 'fly-by-wire' with the throttle position sensor. The 'shark fin' fit perfectly where I removed the brake booster venturi from the intake tube. I may take the car to the drag strip in Tulsa and do some progressively stronger runs to finish off the engine.
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