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			I decided that, rather than start a new thread, I'd pick up where I left off here.   
 
so, since the last post, below; 
 
This has become a mostly-track-use car.  DE's only, as I've promised myself no racing.  (I spent waay too much money racing Superbikes for 20 years..... I won't do that again) 
 
Around June of '18 I had a catastrophic clutch-failure at the racetrack.  Holes in the bellhousing, etc.   
In true-racer-form, I looked at repairs as a time to upgrade, so in went the AASCO LightWeight FlyWheel and new SACHS clutch.  While I was int here I did a RMS and replaced a PERFECTLY-GOOD IMS.   
 
I followed-up with a Underdrive Pulley so the Power Steering would get a break at the track.   
 
Back out and had fun.  Near the end of the year (October?) I took a spin and perhaps didn't get both feet in before it rolled backwards.  I popped a plug outta the heads and the resulting inability to create vacuum meant the AOS was ingesting liquid oil straight into the motor.  I shut down, but nt before the exhaust was saturated enough that it caught on fire.  fun story.  haha.  Anyway.... back to the garage. I dug into the motor enough to discover I had what I think was a recent motor.  it showed ZERO signs of being a 147k mile engine.  And thankfully it wasn't broken.  
 
Over the next winter, (2018-2019) I went through the car again, doing water-pump and thermostat, coolant, etc.  I cleaned-out the debris between the radiators.  I changed-out the oil in the trans and added the 2nd-gear detent fix.  I also installed the 987 airbox and 78mm TB.  To this I added the SOUL Muffler ByPass valves.  Then I installed some FVD adjustable LCA's in the front and took it to have a proper track alignment done (with lots of camber).   
 
The 2019 season was a fun one.... I had a lot of fun passing other "faster" cars.  People say nobody wins practice, but I did.  haha.   
Middle of the year (July / August?) I was railing hard, when I noticed a little "rattle" at  maintenance throttle, or right at pickup.  I couldn't get it to duplicate it in the pits, so I went back out.  It was ever so faint; enough that it was possible I was imagining it.  But I had had enough fun for the day, so I picked-up and started the 30-minute drive home.  10 minutes into that drive it was over.  The motor was done.  Rod-bearing failure.  I'm very certain it happened at what we call the "BlackRock Hairpin" at UMC.  It's at the end of a VERY fast set of left-hand kinks (where I pull the most lateral g's of anywhere on the track) and then a short straight-away, then a hard-braking zone to a 1st gear left-hander.  So the oil is all pushed-away from the pickup, then I'm zinging the down-shifts, way up in the RPM range, then pulling HARD through and out of the turn.  Yeah.... poor guy... (the motor, I mean).  
 
So I bought a crashed car with 80k miles and took the motor out of it.  Parted the rest.   
Over that winter (2019 - 2020) I installed the motor and did the following upgrades: 
 
Replacement Transmission 
Ohlins R&T "Track Package" Coilovers 
Tarret GT3 sway bar & end links in front 
Tarret sway bar and SPL PRO end links in rear 
Adjustable thrust arms in front 
Adjustable toe-links in rear 
Remote-fob-controlled switches to manually turn on the engine-bay purge fan and the radiator hi-speed fans.  (the same fob now controls the SOUL Bypass valves, as well) 
Headers and Mid-Pipes 
 
Cosmetically;  
Replaced the door micro-switches so the windows would drop correctly when the doors opened.   
Fixed the Foam on the doors in the A/C - Heater.   
Wrapped the exterior with vinyl. 
Added Joe Toth spoiler 
Added SideSkirts 
Added GT3 Front lip 
Enlarged the center-hole of the bumper to increase air-flow. 
18" wheels with Fred's center caps.   
 
and Dozens of other little things.
		 
		
		
		
		
		
		
		
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