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Old 06-12-2013, 11:04 AM   #10
navair
Registered User
 
Join Date: Jun 2006
Location: San Diego
Posts: 162
Man, is this a chronic problem I went through the same drill last weekend, second switch in 2 years/10,000 miles! The last time was done by my Indy for an exorbitant 3 hours of labor going in through the dash top ("we dont get under, or we'll have a workman's comp case"). I removed the seat and that made it doable from underneath (with a jewlers screwdriver hacksaw shortened). And of course I found I needed to order torx female sockets to get the seat off (a 3/8" 12 point is close, but was starting to round the seat bolts).
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