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Another view of the "contraption" with its rubber cap removed:
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So far the two ballsocket pieces I've inspected closely in this area seem to be great shape (except from being dirty and dry and in need of some grease, which I will do). The molded-in rubber vibration isolators do deflect under force, but this is by design, the rubber isn't torn or cracked, and don't look bad.
The plastic ballsocket liners although dirty and dry, seem nice and tight with no slop. So I will clean them up, grease them with some badly needed DuPont Krytox PFPE grease, and reuse. |
Please make a DIY :)
Edit: I didn't see the rest of the pictures when I posted this :) |
Can't wait to hear how it works once reinstalled!
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What did you do to replace the bushing?? I would like to improve this spot too.
Good work BTW !! I have 2 cables from Woody and some heim joints on the way to see how hard it would be to replace the cable ends and eliminate some slop as well is the flex that is occurring with the plastic/rubber ends. EDIT: Look what showed up in the mail this morning. http://i70.photobucket.com/albums/i1...psq7vigc7f.jpg These are 6mm Stainless Steel Heim joints with bronze inserts and a grease fitting (small brass bump on the side) too keep them smooth. I can now begin the cutting and threading now that the Box is out of the shop and on it's way to live in VA with my daughter. I have pushed a new project into the shop tho, I'm addicted to cars and will always have 3-4 projects ongoing.... http://i70.photobucket.com/albums/i1...pse9qoitw3.jpg My car interests know no bounds!!! |
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Thanks for the feedback and encouragement, guys!
I took it for a test drive and found an immediately noticeable improvement to shifting, and joy of shifting. Although still not completely perfect, it makes it noticeably more enjoyable to shift, especially on any gear change that involves lateral movement. I'd say subjectively, this change removed 33% of the lateral movement play at the knob. Another 33% improvement I think I can remove by fixing some remaining play I still know about and haven't fixed yet in the shift console mechanism, and I think the last 33% if it could be removed at all, would be inside the transmission itself (so I will live with that, and not expect to remove that last bit.) I've already removed quite a bit of play in the original shift console by freshening the shift console to a low-miles, 997 version with basically zero-play gt3 aluminum bushings, so this is definitely all going in the right direction. :) I made a video showing the zero "contraption" play: trim.27F274F5-B282-4608-8093-0279573704D5.MOV - Video - VideoSprout I bought a couple 10mm all-metal ball socket joints, and tried sticking those on the factory ~10mm ball studs, but found them to relatively sloppy fit (perhaps with 0.005" or play or so) compared to the factory plastic ballsockets which had no noticeable play, it seemed like a step backwards. (check out the video... You can see that the tiniest movement at the shift cable is now being immediately translated through the contraption to rotational movement at the transmission input shaft.) And also, attached is a different view I took of the contraption. This shows after being cleaned up and reassembled. There was a bit of motor oil (or perhaps tranny fluid) on the transmission input shaft and connecting bracket, which I cleaned up, and which I initially was concerned about possibly could have degraded the rubber around the ballsockets, but after inspecting them all (three of the four by removing them and cleaning them up in the process) I think they are all fine and are not contributing any play on my particular transmission. As far as I could tell, front-back movement was being translated relatively immediately (through the single, rubber-isolated balljoint fitting) to in-out movement of at the transmission input shaft. |
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So I tried fixing both of those issues, I think with success. First, I pressed out the bronze bushing using a socket that fit fairly tightly. Tapped it out with a hammer. Then, I basically axially compressed the bushing, carefully, in the vice. This did I think 2 things: 1. It rolled into a "mushroom" shape the thrust surface, making more thickness than it needed to be. 2. It also seemed to have compressed the walls, thereby thickening them. After I reinstalled the "squashed" bushing (by basically pressing it back into the bore with the vice), initially the pivot shaft was a very tight fit - so tight that I think I had to press it in using the vice also - and I found when doing so, it even shaved off some bronze material on the ID near the thrust bearing end! Eventually after working it for a while, and installing it backwards (it seems to have a slight bit of taper, so this helped) the ID of the bushing wore into what I considered near-ideal tolerances. To fine-tune the thrust surface thickness, I got it very close just by using the vice to press the mushroomed thrust surface flatter (with the pivot shaft while pressing with the vice). Eventually I managed getting the e-clip in, but was tight. A bit more thrust surface vice-press flattening, I could get the e-clip on and it was only a little bit tight. At that point, I just worked it rotationally to try to break the thrust surface in, by wearing them without any lubrication, to perfection. (The mating pieces were relatively hard stainless steel, so I wasn't worried too much about them wearing down.). Noticing where the bright spots were where the thrust surface was making contact, I did a bit of sanding (400 grit initially) on the bright spots to help the thrust surface to develop the desired flatness and dimension. I believe this operation is called 'hand scraping' a bearing. Eventually I got it such that, although gravity wouldn't move the bellcrank by itself, a very (I thought acceptably) small amount of rotational torque would, and I called it good at this point. At some point I also added grease, of course. I expect it may wear in a bit further and the small amount of friction that is there may decrease or perhaps eventually even completely go away. Luckily, it's not too much friction to impede the shifting process - it works great and the spring that returns the shift knob to the center gate easily enough overcoming all friction during 2-3 and 5-4 shift motions. (The 2-3 gate movement, if it doesn't work correctly, can easily cause a very expensive "money 2-1 shift"! So don't rush getting enough friction out of this critical system before calling it good. But at the same time, don't rush to remove the friction too quickly or you can overshoot, and have the slop back in there that you wanted eliminated. PS - attached picture shows the heat shield which the "contraption" is behind. Two 10mm nuts removes this heat shield, and you don't even need to jack up the car to do this job. :D Another tip I've learned is to be careful when prying off the ballsockets! Lots of force is required (when dry at least - before getting some grease in there) and if using a pry tool, it's possible to scar up the ball studs if you're not careful. Don't let a metal pry tool touch the ballstuds. And if you scar up the bearing surfaces, sand or file them smooth before reassembling. |
Did you by chance make a measurement of the hole and pin?? as well as the shoulder?
You don't mention them.... |
Sorry; I didn't get those measurements. My battery powered calipers were out of batteries.
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After driving around with the optimized "contraption" for a bit over a week now (with a couple road trips), I've got to say the increased satisfaction of shifts is still there, just like I just did the job yesterday! The wife also immediately noticed and commented on it after her first drive after I did the work - so I highly recommend other manual-transmission boxster owners who want joyful driving have this "contraption slop" tested, and consider eliminating it.
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Interesting!
This is something I need to do! The heim joints solution looks good too! Just need to protect them, they will wear quite fast if you don't :/ |
http://986forum.com/forums/attachmen...lay-image.jpeg
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The foil was simply cut to the length of the shaft and cut to one circumference of wrap. I also cleaned and lubed the cable ends and selector rod ends. 4 ends all together. My shifter is back to original operating crispness and precision. Next step is to rebuild the shifter console with the Function-First Shift Right kit. At that point the whole thing will be better than new. Anyone looking to restore precision and crispness their 986/987 shift should start with this bracket first. Porsche sell an update bracket for over $350. I just updated mine for free. |
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Sent from my POCOPHONE F1 using Tapatalk |
So, bumping this because I have the same issue well documented already here. I swapped for a short shifter but it didn’t make much of any difference—it seems that most of the side to side slop in my 987 is courtesy of racking movement at the linkage pivot shaft as discussed by jakeru and watsongrg.
I tried the aluminum foil trick and it didn’t do that much for me. I think I’m going to try thicker stainless shim stock and see if that makes a difference, or pressing out the bearing. |
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